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Испания аннулировала контракт на поставку авиабомб Саудовской Аравии Citat:Недавний авиаудар возглавляемой Саудовской Аравией коалиции в Йемене привел к тому, что Министерство обороны Испании аннулировало контракт стоимостью 9,2 млн. евро на продажу Эр-Рияду 400 высокоточных авиабомб.
http://www.armstrade.org/includes/periodics/news/2.....tail.shtml
Citat:Tests like these brought on the evolution of “EJECTOR FEET” in the bottom of weapons release racks, or otherwise stores release racks. One of the most popular, was the MAU-12 bomb rack. When the pilot pressed the pickle button, a 27 volt charge hits the primers of 2 impulse carts (similar in appearance to 12 ga. shotgun shells). The gas pressure expanding from their firing not only opens the 2 hooks that grab the bombs lugs that hold it in place, but the pressure sends 2 solid stainless steel rods about 10" long to strike the top of the weapon extremely hard, so as to knock the weapon away from the aircraft, as well as open the retaining hooks. No more tail or stab strikes. I was a Weapons Systems Specialist in the USAF. Decades later, I still remember all this shit, but barely remember what happened freakin’ yesterday! Life gets pretty weird when you get old.
Citat:Second airplane in video, F-105, had bomb bay for carrying nuke internally. Rather than using explosive cartridges to power the weapon away, as was done on wing stations, a large actuator in the top of the bomb bay was charged with nitrogen gas at 225 psi. The bomb rack was bolted to the bottom of the actuator. A gas valve tied to the bomb release circuit unlocked the actuator and allowed it to shove the bomb out with plenty of separation. It worked quite well.
Citat:I was doing intercepts of bogey aircraft in the Texas Air Guard when a wsem (weapon system evaluation missle) came unglued from the rail. Evedently the weapons mechanics loaded it incorrectly or the rail lugs failed (I had done the preflight and shook the missle clone to ck it ) anyway, when it unassed itself, it nosed up and struck the rt elevon. The aircraft left controlled flight with an immediate 40 degree pitch-up resulting in a subsequent stall and spin. After 4-1/2 turn nose down spin, I and 8000' I got it back. Besides a split in the elevon and hinge assembly , there’s was no other damage except I believe the seat cushion had to be surgically removed from my ass. I bought the drinks in terms OC that night. I spent the next 4 days writing reports and signing the -1 paperwork.